Case Study 2:
Reduction of Exposure to Chromate-Based Primer
Background: The manufacturing process evaluated was a
rework operation that involved sanding of chromium-based paint
primers to achieve adequate surface characteristics for
subsequent painting steps. Parts received
from subcontractors had surfaces that were not uniform and had
chips that had to receive additional sanding prior to being
assembled or receiving the final surface painting.
Failure to address the inadequacy of the primer coat
could result in quality issues in the finished products
resulting in further and more costly rework later in the
manufacturing process or, potentially, after receipt by the
customer.
Hazard Identification
The imperfections in the primer coat had to
be hand-sanded by manufacturing operators, resulting in
additional in-process rework and potential chromate exposures to
employees. The danger of chromate dust
exposure was well-recognized by the company and adequate steps
were taken to provide and use personal protective equipment to
ensure worker safety. Previous sampling
exposure monitoring determined that unprotected worker exposure
to airborne hexavalent chromium was five times the permissible
exposure limit (PEL) when spraying the primer, and two times the
PEL during vacuum sanding. In addition, OSHA
had recently issued a new standard revising the current PEL
downward (to 1 microgram per cubic meter of air as an 8-hour
time-weighted average), thus putting additional focus on the
chromium exposures at the facility.
Hazard Intervention
The company had long recognized the hazard
associated with chromate-based paints.
However, in complex operations many priorities compete for
management’s time and focus. Since employees
were receiving adequate protection from local exhaust
ventilation and PPE,
there was no sense of urgency to find options to eliminate the
use of chromate-based primers.
The IH-generated project provided impetus
to the re-evaluation of the requirement to use chromate-based
primers in the aircraft manufacturing process.
The project required both time and resources from the
production and engineering staffs to demonstrate that
non-chromate based primers would be adequate substitutes to
ensure a high level of both product quality and employee
protection. Once the testing was
satisfactorily completed, additional costs were incurred to make
the design change to the product specifications and communicate
the changes to the appropriate sub-contractor.
Impacts of the Intervention
The new priming material reduced paint
chipping, which resulted in improved quality of the
primer-coated parts. Along with a concurrent
project to address the quality of vendor-produced parts,
eliminating the need to rework chromate-primed parts resulted in
a significant labor productivity savings.
The intervention eliminated worker exposure
to chromate dusts from rework sanding.
Employees were still exposed to non-chromate dust, but as a
result of the intervention the level of respiratory protective
equipment required could be reduced from full-face powered
air-purifying respirators (PAPRs) to half-face air-purifying
respirators.
As a result of the elimination of chromate
dust, the company was also able to avoid implementing costly
changes to the facility’s exhaust ventilation systems.
The new hexavalent chromium standard would have required
a more robust ventilation design to comply with the 2010
compliance date for the new OSHA PEL. Without
the need to comply with more stringent requirements, existing
exhaust ventilation systems were deemed acceptable or would
require significantly fewer design upgrades to meet company IH
standards.
Other benefits of the intervention
included:
1. Increased customer satisfaction due to product deliveries
that required less follow-up surface rework
2. Elimination of chromate primers improved a corporate
social responsibility metric associated with corporate Materials
of Concern (MOC)
3. Increased employee morale due to the elimination of
chemical exposures greater than the company’s occupational
exposure limit (OEL)
4. Decreased regulatory risk due to the elimination of
hexavalent chromium in this operation
5. Lessons learned from the project have the potential to be
transferred to other products and facilities within the
corporation.
Financial Metrics
A ROHSEI analysis was conducted on the
benefits and costs associated with the intervention.
The analysis showed that the substitution of non-chromate
priers resulted in an after-tax net present value savings of
$504,694 over the 5-year duration of the project evaluation.
This represented profit that could be attributed to an
additional unit of production per year. In
addition, the substitution resulted in significant productivity
gains.
Lessons Learned
A key lesson learned for the project was
that in some cases management is aware of the need for certain
actions but is distracted by a multitude of other issues
associated with operating the business or organization. In
addition, even in highly responsible organizations management
may delay taking action if they have the perception that
employees are adequately protected by
PPE. In this case
management knew the right thing to do and the project should
have proceeded on its own merit; however, the project did not
rise up the company’s priority list until the proper management
focus was created by IH professionals.
IH professionals can be catalysts to enable organizations
to make process or business changes that not only protect
employees but also result in significant business improvements
that can save money and contribute to an organization’s
competitive advantage.
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